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 Life of Well Solutions

TAM delivers responsive service to keep you up and running. Inflatable technology experts with a 50-year track record of innovation, we’re the ones you call when you have an intervention challenge or complex issue downhole. We offer the right tools for the right applications to solve problems and get you back online quickly and accurately. Nimble and collaborative, we partner with customers to drive our internal R&D programs. From drilling & completions and well intervention to unconventional resources and reservoir optimization, TAM has the well integrity solutions to maintain your excellence at the wellsite.

Large Diameter Casing Solutions
Case History: Gulf of Mexico
Leak hunt in 22 in. casing. A deepwater Gulf of Mexico operator was unable to get a successful positive test from their 22 in. casing across their 16 in. liner top. The TAM-J Multi-Set Inflatable Packer dressed with TAM’s 15.10 in. Dual -Anchor Element was utilized to ensure the leak was not located within their 22 in. casing. TAM set the packer immediately above the 16 in. liner top and tested twice from above, proving the integrity of the 22 in. casing. These tests identified the leak point as the 16 in. liner top. The leak was later successfully squeezed and the drilling operations continued.

Large Diameter Casing Solutions

Thru-Tubing Solutions
Case History: Scotland
A customer in Aberdeen wanted to isolate water production behind a 4-1/2 in. slotted liner. After several failed attempts, they called TAM. A TAM Thru-Tubing Bridge Plug and Cement Retainer were deployed on coiled tubing to successfully shut off the water zone.

Thru-Tubing Solutions

P&A Solutions
Case History: Gulf of Mexico
A Deepwater Gulf of Mexico Operator had a multiple well P&A project and was required to set an approved barrier in 20 in. casing. A base-of-cement bridge plug was required to ensure the cement was spotted successfully. TAM set a 5.06 in. OD TAMPlug dressed with our 14.50 in. OD VE Element; all inflatable bridge plugs set successfully. The balanced cement plugs were spotted successfully and tested from above in one trip in the well. This application showed the operator value by ensuring all cement plugs remained in place, saving time and money on potential remediation costs.

P&A Solutions